It's more like "spot the difference" really, but regular followers will observe that the transition from wood to plastic has commenced. I've replaced my wooden x-axis components with newly printed plastic (PLA) ones. As I've become more fussy about print quality I've realised a little looseness here and there, and tiny wobbles in the z-rods were showing up as patterns in my printing. I've printed quite a few components for a complete new RepRap at this stage, but with the accuracy of some components now being impacted I chose to do an interim rework of my repstrap.
It's got a new x-end idler. This one http://www.thingiverse.com/image:63587, but instead of fitting real LM8UU linear bearings, I've fitted these printable PLA substitutes http://www.thingiverse.com/thing:12238. We'll see how that experiment goes!
Now, just to mix it up a bit I've put the more traditional x-end motor bracket, http://www.thingiverse.com/image:63177, on the far end, but I've modified it slightly. I'm only using one nut on the z threaded rods. Can't see the point of the second nut and the spring between them. I know it's an anti-backlash design, but I've had only one nut in my wooden design and gravity looks after backlash in the vertical direction. I've no plans to print in zero gravity. :-) Also I couldn't bring myself to use that overhanging motor design, so my motor stays inboard for a more balanced look.
I've retained my wooden z-motor brackets and vertexes(?). They are solid and accurate.
The x-carriage and extruder is now fully RepRap, and as you can see from the part on the bed, I'm printing a spooler!
But a key part of improving print quality has been a fresh examination and fine tuning of basics like squareness, perpendicular z-rods, frame triangle distances all equal. I've screwed the unit to a base board to increase rigidity also. Finally, the introduction of better belt-tensioning technique such as found on Gregs x-carriage, and this little unit (http://www.thingiverse.com/thing:10274) have been invaluable in removing print quality issues due to backlash. The use of these fine tuners allows belt tension to be adjusted a little at a time without over tightening, that might strain something else out of alignment.
Here's a quick look at two test pieces fresh off the newly rebuild rig. I'm pleased with the current print quality.
Now to make it go faster! :-)
Happy printing!
Nice Job. It will be a shame to see the Oak go, I think it's really nice. That's some good upgrades mind, and your prints are looking great!
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